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NickD
NickD MegaDork
2/18/25 3:19 p.m.

Anybody want some RDCs? Ozark Mountain Railcar has a solid dozen for a cool $6,096,000. These were the Trinity Railway Express' units that were purchased by AllEarth Power, a solar panel manufacturer based in Vermont, who owned them under a subsidiary called AllEarth Rail. AllEarth was pushing for VT commuter rail from Burlington to Montpelier and St. Albans. AllEarth Rail wasn't going to operate these services, they just wanted the local governments to operate the service and then lease the RDCs from them. Not one entity in Vermont took up that challenge, since the towns are so small that it was hard to justify commuter rail, especially since they are not even collinear, meaning a separate route for each, and it was cheaper and faster to drive. AllEarth then leased two to Finger Lakes Railway, one for use on the Finger Lakes itself, and another for use on FGLK's Midcoast Rail Service in Maine. The one at Midcoast suffered some sort of failure, both RDCs went back to AllEarth, and then AllEarth was reportedly going to sell them to Société du chemin de fer de la Gaspésie (Gaspésie Railway Society, reporting mark SFG) for use in excursions in Quebec. But they were unable to get the funding together and the RDCs are for sale again.

https://ozarkmountainrailcar.com/railEquipment.php?itemId=4122&category=Passenger%20Equipment

 

Pete Gossett (Forum Supporter)
Pete Gossett (Forum Supporter) MegaDork
2/18/25 3:50 p.m.

In reply to NickD :

Half-mil each seems a bit pricy to me?

NickD
NickD MegaDork
2/18/25 8:05 p.m.

In reply to Pete Gossett (Forum Supporter) :

I mean, Nevada Northern just paid $400,000 for that Brill M-55. Trinity Rail had the RDCs pretty heavily overhauled and upgraded in 1997 when they got them, including replacing the obsolete Detroit 6-110 motors with modern Cummins engines, and they are fully compliant with modern standards. Honestly, the biggest issue I see is that it seems like selling the full dozen as a solid batch might be a tall order. 

Duke
Duke MegaDork
2/18/25 8:46 p.m.

NickD
NickD MegaDork
2/19/25 9:16 a.m.

In reply to Duke :

The crazy part of this is that the Bangor & Aroostook had those EMD F3As, purchased in '48, and EMD BL-2s, purchased in '49, still operating well into early '90s, well after they had vanished on every other Class I, and pretty much every short line as well.

NickD
NickD MegaDork
2/19/25 9:18 a.m.

The Bangor & Aroostook, in Cleveland?!  In 1950, BAR wanted to fully dieselize, which it did in 1951, with 42 units replacing 73 steam engines, but each winter when the Maine potato crop began to move, it found itself having to fire up stored steamers. So the BAR solved the problem in a unique way: It ordered 12 GP7s but signed a seven-year pact to lease 10 of them, at no profit, to the Pennsylvania Railroad during each May 1st to November 15th period. The deal was extended, and carried on into the ‘70s, as evidenced in this June 1961 scene on Cleveland’s Lake Erie waterfront, where two of the GP7s and three of its five GP9s congregate in front of Municipal Stadium. BAR power was pretty common throughout the northeast, as other railroads, notably Conrail, D&H and NYS&W, would also lease their motive power during the spring and summer.

02Pilot
02Pilot PowerDork
2/19/25 9:50 a.m.

In reply to NickD :

I seem to recall seeing one of those BL2s in B&A colors in Honesdale, PA some years ago. Strange looking engine.

NickD
NickD MegaDork
2/19/25 10:47 a.m.

In reply to 02Pilot :

Yep, the #54 at Delaware, Lackawaxen & Stourbridge, once a D-O Corp. operation. I remember seeing it when I drove through Honesdale back in 2017 with Wally, while crewing for Empire State Performance Rally, and then I rode it, and took this photo, in '22. I had chased the first Ramble with #2102 on Saturday, and then swung through Honesdale on Sunday on the way home. They used a Pennsy FP7 on the other end. Not a bad trip, but not a standout.

NickD
NickD MegaDork
2/19/25 10:54 a.m.

I have always been baffled why EMD went the route they did with the BL2 in 1949, when Alco had introduced the road switcher with the RS-1 in 1940, and Baldwin and Fairbanks-Morse had also rolled out their respective DRS-4-4-1500 and H-15-44 road switchers in 1947. The only thing I can think is that either EMD, who was the innovator of the diesel locomotive, didn't want to be perceived as copying the competition, or, since this was the Harley Earl era at General Motors, the road switcher was viewed as too plain and utilitarian.

NickD
NickD MegaDork
2/19/25 12:17 p.m.

The irony is that while BL2 was a sales failure for EMD, with only 58 built (plus one BL1, which is a confusing subject), but 7 of them are preserved. Compare that to the EMD E7A, which sold 428 units and only one of them is preserved. Part of that is because, despite not being a great unit, they lasted quite long for a lot of their owners, especially BAR.

Duke
Duke MegaDork
2/19/25 12:49 p.m.

Horseshoe Curve:

NickD
NickD MegaDork
2/19/25 4:10 p.m.

In reply to Duke :

I've been there. Twice, actually. Even caught the PRR heritage unit, sadly not leading. It's pretty impressive, watching the trains climb from the north side, engines thunder and flanges screaming, then wrap around you and continue up the south end. Also the only place I've been with dedicated helper units, and at the right time of day, it's a flurry of activity. And that's in the modern, sanitized Norfolk Southern age, with lookalike widecab EMDs and GEs everywhere. I can't imagine what it was like in the steam era under Pennsy, with I1 2-10-0s and J1 2-10-4s fighting with freights, and T1 4-4-4-4s and doubleheaded K4s with passenger trains. Even in the diesel age, it had to be fascinating, with those freakish Baldwin DR-12-8-1500/2 "Centipedes" or big Alco RSD-12s in helper service.

 

NickD
NickD MegaDork
2/20/25 9:42 a.m.

This popped up in Youtube, a corporate promotional film by the Central Railroad of New Jersey. A lot of very cool footage in it; cars with Central Railroad of Pennsylvania reporting marks, the Huber Breaker and Ashley Planes cable railroad, the rotary dumper at Jersey City, the Newark Bay Bridge, and for me it was really cool to see the CNJ line from Penobscot to Mauch Chunk (Jim Thorpe), including the operational PQ Tower at Nesquehoning Junction, which I've ridden and photographed. These old promotional films are also an interesting look at a time when railroads were part of a the public conscious and newsworthy, unlike now where they mostly exist in the background until there's a derailment. I've seen news articles from newspapers remarking when railroads took delivery of new equipment, and I remember stumbling across old news reel footage of the DL&W inviting local Scranton press to come check out their freshly delivered 4-8-4 "Poconos" and go for a ride behind them.

 

NickD
NickD MegaDork
2/20/25 12:45 p.m.

That Newark Bay Bridge was the site of a pretty horrific incident on September 15th, 1958. The lift-span bridge had three signals, spaced at 3⁄4 of a mile , 1⁄4 mile of a mile, and 500 feet from the bridge, and an automatic derailing device 50 feet beyond the third signal. The bridge span had to be down and locked electrically before the signals and derail could be cleared for movement on the track, and also all the devices had to be in their most restrictive positions before the bridge could be unlocked and raised.

CNJ train number #3314 was a morning commuter service from Newark to Manhattan consisting of two CNJ GP7s, #1532 and #1526, and five passenger cars, with 63 year old Lloyd Wilbur as engineer and 42 year old Peter Andrew as fireman.  At approximately 9:45AM, a dredge approached Newark Bay, and since it wouldn’t fit through the 35ft gap below the lowered bridge, an order to raise the lifts was issued. The control center, located in the middle of the bridge between the lifts, turned all the approach signals red, engaged the derail, and raised the lifts up just as CNJ train #3314 approached the bridge from the west at 40mph. The approach signal for the bridge dictated a 20mph speed limit, standard for an approach to a red signal.

By 10:00am the train entered the western side of the bridge, still traveling at 40mph, and disregards the red signals. At the same time the dredger for which the bridge was opened reaches the lifts. CNJ train #3314 hit the derailer at full speed, never making a speed reduction or attempting to slow, and while derail did work, the train's higher speed it carries on right to the end of the fixed section of the bridge. It ran out of bridge, fell over the edge, and plunged 40ft down into Newark Bay, narrowly missing the dredge. The second locomotive follows the leading unit, and pulls the first two passenger cars to their doom. The third car, tearing off the car in front, tips over the edge but is saved by its rear truck becoming stuck on the edge, leaving it dangling from the edge of the bridge at a steep angle. The two locomotives and leading two passenger cars sink in an instant, disappearing below the water as soon as they fall in. 46 passengers drown in the leading two passenger cars, along with the both the crew in the leading locomotive. Another 48 passengers are injured as they escape the submerged train cars or the third car as it dangles from the edge.

All passengers in the third car manage to climb to safety, making it onto the bridge as the first responders arrive by boat or by running up the bridge on foot. The rear truck of the third eventually gives out, dropping the car into the bay 2 hours after the accident. Divers go down to the wreckage to count victims, while other responders search the shore downstream for further victims and survivors. They didn’t find anyone, since those who had died hadn’t even left the train. It’s assumed that most passengers likely didn’t know that something was wrong right up until the train hit the water.

 

The The ICC, Army Corp of Enginers and New Jersey Public Utilities Commission all conduct separate investigations, and the bridge operator was found to have done his job properly, and the signals and derails were in operating order. The derail failed to save the train simply because they hit it at twice the intended speed. They raised the wreckage and did not find any defect of the braking system on the locomotives and coaches. An autopsy found that the engineer had indications of hypertension, but he had died of asphyxia due to drowning.  It was presumed that the engineer had somehow become incapacitated in the cab, but no reason could be found to explain why the fireman could not or did not step in to stop the train. The cause remains a mystery to this day.

All three investigations found that the absence of a dead man's switch was one primary cause of the crash. After the inquiries, the New Jersey Public Utilities Commission ordered the railroads to install such devices on all passenger locomotives operating in New Jersey. Some CNJ locomotives were already equipped with such devices, but this did not include the the lead engine, #1532 on the day of the wreck. The CNJ had previously claimed that such a device was not always necessary, because all their trains had two crewmen in the locomotive cab, and if the engineer was incapacitated somehow, the fireman would assume control of the locomotive, which obviously didn't happen in this case.

The two locomotives, #1532 and #1526 were raised, rebuilt by EMD into GP9s, and returned to service. The #1532 retained its original number, while the #1526 was renumbered #1531. They were regeared and had their passenger equipment removed and served primarily as freight locomotives, although #1532 was photographed in passenger service after its return from EMD and they were also seen hauling commuter runs early in the Conrail era. Both engines were renumbered into Conrail numbers, as #5678 and #5679, although I don't believe they ever wore Conrail blue and they were retired and scrapped in '84.

As for the bridge, it was in the news again on May 19th, 1966 when the French freighter S.S. Washington collided with the northeast lift span, rendering two tracks unusable. Despite an eventual judgment in CNJ's favor, the span was never repaired, as the two affected tracks were deemed redundant by the railroad due to the sharp decline in rail traffic and the impending Aldene Plan, which occurred less than a year after the accident, would also completely alter CNJ passenger operations. After the Aldene Plan went into effect in May 1967, the only passenger service on the bridge was the Bayonne-Cranford shuttle, known as the "Scoot". The last freight train crossed the bridge in 1976, prior to the formation of Conrail, and the last passenger train left Bayonne's Eighth Street Station on August 6, 1978. Demolition of the central lift spans began in July 1980 after the Coast Guard declared the structure a navigational hazard to ships. The trestle and approaches were removed in 1987–1988 and removal of the piers began in 2012.

 

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